Page 21 of 21

Posted: Thu Sep 04, 14 11:43 pm
by mopar_mark
Cannonball wrote:watch street outlaws you will chuck that 700 double pumper in the bin,,,, :roll: :roll:
:D :D :D

Posted: Sun Sep 07, 14 3:23 pm
by GJUK
mopar_mark wrote:
Cannonball wrote:watch street outlaws you will chuck that 700 double pumper in the bin,,,, :roll: :roll:
:D :D :D
I've seen a couple of these this week and yeah, I need to turbo my car :D

Posted: Mon Sep 08, 14 1:34 am
by Dave-R
GJUK wrote:17 degrees of advance at idle SHOULD have been spot on.
I dial 19-20 degrees into a STOCK 440. My own 440 with bigger cam I had 25 initial and 35 total.

Posted: Mon Sep 08, 14 9:08 am
by GJUK
Dave wrote:
GJUK wrote:17 degrees of advance at idle SHOULD have been spot on.
I dial 19-20 degrees into a STOCK 440. My own 440 with bigger cam I had 25 initial and 35 total.
I got the timing light on the car and it is showing 45 degrees initial timing at idle.

Needless to say something is incorrect, the timing light or the timing mark.
Or maybe the Damper is slipping (thigh I can not see it is doing that).

The car went out again yesterday for a 10 mile jaunt. Ran well, 180*F max, it was quite a warm day as well. Pulled like a train, idled well even after a sharp stop from 70mph.

Perhaps someone will be able to spend 30 minutes on it with me at HRD's and show me where I've gone 'wrong'?

It is leaking coolant now though lol. Always something eh.

J

Posted: Mon Sep 08, 14 9:36 am
by Guy
Find me mate I will have nothing to do and will look over it for you on the saturday

Posted: Mon Sep 08, 14 10:24 am
by GJUK
Guy wrote:Find me mate I will have nothing to do and will look over it for you on the saturday
:thumbright: :thumbright:

Posted: Mon Sep 08, 14 12:52 pm
by Dave81
GJUK wrote:
It is leaking coolant now though lol. Always something eh.

J
The joys of Mopar ownership.......... :D

Posted: Mon Sep 08, 14 1:03 pm
by GJUK
Dave81 wrote:
GJUK wrote:
It is leaking coolant now though lol. Always something eh.

J
The joys of Mopar ownership.......... :D
I knew it would never be cheap but DAMN its swallowing up cash.

New charging system, new sump, refurb on the gearbox thingymajig, ne gauges, full cage, leafs moved in, carb, ht leads, plugs, exhaust...

:D Love it.

Posted: Mon Sep 15, 14 2:26 pm
by GJUK
'Final' update on this thread in case it helps others in the future.

TDC was found again at Hot Rod Drags by the best pit crewe I've ever encountered!
Rocker cover off, inlet and outlet rocker when they can move means its at TDC on compression stroke.
checked the mark on the damper, it was not correct.
wiped off and remarked.
I think the car was running 25-27* advance at idle then nearly 50 at full load at 3krpm.
There was 15 degress of advance in the dizzy so this has now been changed to 17* at idle and 32* advance at full (I think, I'll need to check. I was that excited it was running well I can't remember!)

So the carb was a problem that caused the bogging and total cut out due to over fueling, fuel fountains etc. Floats fixed that issue.

Then the Timing was out and it had too much when at total advance.

Drove home really well, in traffic it was 185*F on the run it was 175-180*F

Very happy with it.

Thanks guys.

Jon

Posted: Mon Sep 15, 14 3:38 pm
by Charger
result!!

glad you got it sorted

:thumbright:

Posted: Mon Sep 15, 14 5:01 pm
by Les Szabo
Good its all sorted!, would've thought that you could run more than 32 total at your 8.1CR though even on normal unleaded, but no matter.

Les

Posted: Mon Sep 15, 14 5:07 pm
by John
GJUK wrote:'Final' update on this thread in case it helps others in the future.

TDC was found again at Hot Rod Drags by the best pit crewe I've ever encountered!
Rocker cover off, inlet and outlet rocker when they can move means its at TDC on compression stroke.
checked the mark on the damper, it was not correct.
wiped off and remarked.
I think the car was running 25-27* advance at idle then nearly 50 at full load at 3krpm.
There was 15 degress of advance in the dizzy so this has now been changed to 17* at idle and 32* advance at full (I think, I'll need to check. I was that excited it was running well I can't remember!)

So the carb was a problem that caused the bogging and total cut out due to over fueling, fuel fountains etc. Floats fixed that issue.

Then the Timing was out and it had too much when at total advance.

Drove home really well, in traffic it was 185*F on the run it was 175-180*F

Very happy with it.

Thanks guys.

Jon
It was nearer 40 initial and 55 total Jon. We set it at 18 so the total should be a conservative 33. Now you have just the one timing mark ;) you should be able to have a fiddle and see how she performs if you increase gently :thumbright:

Posted: Mon Sep 15, 14 5:28 pm
by GJUK
Ah thanks for clearing that up John.

Well pleased with how its driving for now, might knock it forward a little but will get it marked up on the dizzy so I can return it in case I go too far!

Cheers

Jon

Posted: Wed Sep 17, 14 12:17 am
by GJUK
Here's the A Team in action :D

I think John (Blue) is wiring up some C4 to 'sort' the car up in this photo!

Many thanks everyone.

Jon

Image