I had a short run out to a local meet on Sunday morning with Matt H and it was still the same when I parked up.
However, when I drove back and checked at home, the trans was not as hot and both pipes were very warm for their entire length.
I am going to fit a separate trans fluid cooler (currently on the stock rad lower section) and at the same time I will use the flow test method, Rebel
I also noticed that the kick down lever was, or rather the split pin holding the rod in place, was fouling the gear selector lever on the trans body.
This was preventing the lever going back all the way and also reducing throttle travel so I hope I haven't damaged anything
I have set the kickdown correctly as I've done this successfully before when I changed the inlet manifold so I'm confident this is close and I have now fixed the lever interference issue.
Since installing the new torque convertor (2400 stall), up shifts seem a lot later so I think some fine tuning is now in order when I next get time.
Having just put the engine back together I am reluctant to floor it until I get some miles in
